华电技术 ›› 2013, Vol. 35 ›› Issue (6): 25-29.

• 研究与开发 • 上一篇    下一篇

600MW机组协调控制系统优化

  

  1. (广东红海湾发电有限公司,广东汕尾〓516623)
  • 出版日期:2013-06-25 发布日期:2013-07-23

Optimization of coordinated control system of 600MW unit

  1. (Guangdong Red Bay Power Generation Company Limited, Shanwei 516623, China)
  • Online:2013-06-25 Published:2013-07-23

摘要:

摘要:对汕尾电厂600MW超临界直流机组协调控制系统进行了分析,设计了负荷变化速率(BIR)前馈回路,优化了汽轮机主控制器的汽压修正回路,调整了锅炉主控的控制策略,形成了比较完善的协调控制方案。解决了机组运行时主汽压力波动较大、升降负荷有延迟、机前压力扰动过大、主蒸汽温度容易超温等问题。试验结果表明:协调控制系统优化后,有效提高了机组的负荷响应能力以及安全、稳定运行水平。

关键词: 关键词:协调控制, 锅炉主控, 汽机主控, 中间点温度, 逻辑优化

Abstract:

Abstract:The coordinated control system of the 600MW supercritical oncethrough unit of Shanwei Power Plant was analyzed. The load variation rate feedforward loop for the boiler input rate (BIR) had been designed. The steam pressure corrective loop of steam turbine master control was optimized. The control strategy of the boiler master control was adjusted. A more perfect coordinated control scheme was formed. Some problems, such as that the main team pressure fluctuates greatly, there is certain delay for load increase and load decrease, the disturbance of the steam pressure near the inlet of the turbine is too large, the main steam temperature often exceeds the normal and so on, were solved. The test result shows that after the coordinated control system had been optimized, the load response ability and the safe and stable operation level of the unit were improved effectively.

Key words: Key words:coordinated control, boiler master control, steam turbine master control, temperature of intermediate point, logic optimization