华电技术 ›› 2019, Vol. 41 ›› Issue (5): 50-51.

• 节能与环保 • 上一篇    下一篇

2x1000MW机组除灰系统节能改造

  

  1. 华电莱州发电有限公司,山东莱州〓261400
  • 出版日期:2019-05-25 发布日期:2019-06-04

Energysaving retrofit of 2×1000MW unit ash handling system

  1. Huadian Laizhou Power Generation Company Limited, Laizhou 261400, China
  • Online:2019-05-25 Published:2019-06-04

摘要:

针对华电莱州发电有限公司一期2×1000MW超超临界燃煤机组电除尘气力除灰系统存在气化风量不足、耗电多、故障率高、维护费用高等问题,利用节能改造机会,提出了电除尘器灰斗气化风机与锅炉脱硫氧化风机联合的改造措施,并对改造前后的气化风量、故障率、节能量进行了比较。改造后机组运行稳定,提高了气化风量,降低了设备的维护费用,节能降耗效果明显。

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Abstract:

There is insufficient gasification air volume, high power consumption, high failure rate and high maintenance cost in the pneumatic ash handling system for ESP of 2×1000MW ultrasupercritical coalfired unit in Huadian Laizhou Power Generation Company Limited. Taking advantage of energysaving retrofit, the combination of the ESP dust collector gasification fan and the boiler desulfurization/oxidation fan isproposed. Comparing the gasification air volume, failure rate and energy saving before and after the transformation, it is found out that the unit runs stably, the gasification air volume is increased, the maintenance cost of the equipment is reduced, and the energy saving effect is obvious after the retrofit.

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