华电技术 ›› 2017, Vol. 39 ›› Issue (7): 73-76.

• 节能与环保 • 上一篇    

600MW燃煤机组SCR装置喷氨优化调整试验研究

  

  1. 华电电力科学研究院,杭州〓310030
  • 出版日期:2017-07-25 发布日期:2017-08-08

600MW coalfired unit SCR ammonia spraying improving adjustment test study

  1. Huadian Electric Power Research Institute, Hangzhou 310030, China
  • Online:2017-07-25 Published:2017-08-08

摘要:

以某电厂600MW燃煤机组脱硝工程为例,介绍了氨逃逸的危害、选择性催化还原技术(SCR)装置喷氨优化试验的判断依据以及喷氨优化调整试验的思路、流程及方法。通过喷氨优化调整试验,SCR装置A侧和B侧出口NOx质量浓度分布相对标准偏差由60.8%和28.9%分别降至13.5%和8.8%,氨逃逸质量浓度分别降低了63.4%和53.8%。反应器出口NOx质量浓度分布均匀性得到明显改善,同时氨逃逸质量浓度也得到了控制,提高了机组运行的安全经济性。

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Abstract:

Based on a power plant 600MW coalfired unit denitration project, the harm of ammonia escape, criterion of selective catalytic reduction (SCR) system ammonia spraying improving test and procedure and method of ammonia spraying improving adjustment was introduced. By ammonia spraying improving adjustment test, the NOx mass density of side A and side B outlet was reduced from 60.8% and 28.9% to 13.5% and 8.8%. Ammonia escape mass density reduced by 63.4% and 53.8%. Reactor outlet NOx mass density distribution was improved. Ammonia escape mass density was controlled. The safety and economy of unit operation was enhanced.

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