Huadian Technology ›› 2010, Vol. 32 ›› Issue (2): 29-30.

• 研究与开发 • Previous Articles     Next Articles

Study on improving measures for pulverized coal distribution evenness

ZHANG Huxiang   

  1. Wangting Power Plant, Suzhou 215155,China
  • Received:1900-01-01 Revised:1900-01-01 Online:2010-02-25 Published:2010-02-25

Abstract: Good results have been obtained after reforming the pulverized coal system of #11 boiler in Wangting Power Plant. The maximum deviation of air and coal powder in deferent layer was less than ±10%, which is favorable for the balance of flue gas flow from two sides of furnace outlets, implementation of low NOx emission and steady combustion in boiler lowload. Now flue gas temperature deviations between two sides before hightemperature reheater are controlled in 15℃. No blockage in pulverized coal pipe, no overtemperature tubebursting and other bad phenomenon have been occurred until now, and unburned carbon content in the fly ash has decreased year by year.

Key words: concentration deviation, pulverized coal distributor, optimizing combustion