华电技术 ›› 2011, Vol. 33 ›› Issue (7): 65-67.

• 节能与环保 • 上一篇    下一篇

脱硫增效剂在电厂的应用

彭桂云,朱跃,高正来,程雪山,宋广田   

  1. 华电电力科学研究院,浙江杭州310027
  • 收稿日期:1900-01-01 修回日期:1900-01-01 出版日期:2011-07-25 发布日期:2011-07-25

Application of desulphurization synergist in thermal power plants

PENG Guiyun, ZHU Yue, GAO Zhenglai, CHENG Xueshan, SONG Guangtian   

  1. Huadian Electric Power Research Institute, Hangzhou 310027, China
  • Received:1900-01-01 Revised:1900-01-01 Online:2011-07-25 Published:2011-07-25

摘要: 介绍了某电厂600MW机组脱硫装置使用脱硫增效剂的试验情况。原来需开3台浆液循环泵才能使SO2排放浓度达标,使用脱硫增效剂后,仅开2台循环泵即可使SO2排放浓度达标,电耗可下降951(kW·h)/h,脱硫效率较使用脱硫增效剂前有明显提高。使用脱硫增效剂后,脱硫系统中浆液及脱硫石膏性状并无明显变化,特别是Cl-的质量分数和pH值无较大变化,说明使用脱硫增效剂后不加重系统的腐蚀性且对石膏品质无影响。社会效益及经济效益良好,不会对脱硫系统形成负面作用。

关键词: 烟气脱硫, 脱硫增效剂, 经济效益, 降低能耗

Abstract: The experiment of using desulphurization synergist in 600MW unit desulphurization equipment of a power plant was introduced. Originally, it was necessary to run three slurry circulating pumps to make the SO2 emission concentration can meet the requirement of related standard. After the desulphurization synergist had been used, the desulphurization efficiency was increased obviously, and only two slurry circulating pumps must be run for the same target; the electric energy consumption was decreased by 951kW·h in a hour. After the desulphurization synergist had been used, the characteristics of the slurry in FGD system and the desulphurization gypsum does not vary obviously; especially, the mass fraction of Cl- and the pH value do not vary obviously, which shows that the desulphurization synergist would not enhance the corrosion of the system, and it would not influence on the gypsum quality too. So, the using of desulphurization synergist has obvious economical benefit and social effect, and does not cause negative influence on the desulphurization system.

Key words: flue gas desulphurization (FGD), desulphurization synergist, economical benefit, reduce energy consumption