华电技术 ›› 2009, Vol. 31 ›› Issue (11): 6-8.

• 专题综述 • 上一篇    下一篇

印尼风港电厂炉膛负压自动控制优化

陈霄峰,王孟,杨保卫   

  1. 浙江省火电建设公司,浙江杭州 310016
  • 收稿日期:1900-01-01 修回日期:1900-01-01 出版日期:2009-11-25 发布日期:2009-11-25

Optimization of furnace negative pressure automatic control of Labuhan Angin Power Plant in Indonesia

CHEN Xiaofeng,WANG Meng,YANG Baowei   

  1. Zhejiang Thermal Power Construction Company, Hangzhou 310016, China
  • Received:1900-01-01 Revised:1900-01-01 Online:2009-11-25 Published:2009-11-25

摘要: 分析了印尼风港电厂负压自动控制投入的几个难点,对现场控制设备及DCS内负压自动逻辑进行了针对性的优化,成功地解决了这个难题并经受住了引风机和一次风机RB试验的考验。

关键词: 炉膛负压, 现场控制设备, 负压自动逻辑, 优化

Abstract: Several difficult points during putting the furnace negative pressure automation control of Labuhan Angin Power Plant in Indonesia into operation were analyzed. The field control devices and the negative pressure automation logic in DCS had been optimized. Thus the difficult problems had been solved successfully, and the system stood the test of the RB experiment of induced draft fan and primary fan.

Key words: furnace negative pressure, field control devices, negative pressure automation logic, optimization