Huadian Technology ›› 2021, Vol. 43 ›› Issue (5): 64-69.doi: 10.3969/j.issn.1674-1951.2021.05.010

• Energy Conservation and Environmental Protection • Previous Articles     Next Articles

Experimental study on deep peak-load shaving of a 660 MW ultra-supercritical secondary reheating unit

CONG Xingliang1(), XIE Hong1, SU Yang1, ZHANG Jun1, CHENG Yingjie2   

  1. 1. Anhui Electric Power Science Institute of State Grid, Hefei 230601, China
    2. State Grid Bengbu Power Generation Company Limited,Bengbu 233000, China
  • Received:2020-09-29 Revised:2021-03-28 Online:2021-05-25 Published:2021-05-18

Abstract:

To adapt to the development trend of coal-fired units in the context of realizing carbon peak and carbon neutrality, deep peak-load shaving study was made on a 660MW ultra-supercritical secondary reheating unit. The experiment verified that the unit performs well at 30% rated load. Under 30% rated load, the combustion in the boiler is stable and in good condition. The control and operation parameters of the main and auxiliary equipment are normal and stable with adjustment margins. The environmental protection equipment works well and keeps the discharged pollutant within the ultra-low emission standards of China. However, the economic performance of the unit running with 30% rated load is inferior to that with 50% rated load. Influenced by heat consumption for steam turbine unit,heat consumption for boiler and auxiliary power rate,coal consumption for power supply of the unit running with 30% rated load is much higher than that of the unit with 50% rated load,increasing by 49.0 g/(kW·h).Thus,the parameters of units under deep peak-load shaving need to be further adjusted and optimized.

Key words: deep peak-load shaving, secondary reheating, minimum load for stable combustion, 30% rated load, ultra-supercritical boiler, coal consumption for power supply, carbon neutrality

CLC Number: